Friday, August 27, 2010

Some Notes on Reassembling the BSF S20

Reassembly of the S20 is not easy. Rather than use screws like any normal airgun (with the non exception of the equally abnormal Tempest and Hurricane), the pistol is largely press fit together. So although it needed cleaning, if it worked fine I would never take one apart again.

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Piston head is rough ground.

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Spring end is pretty rough

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Spring guide is downright crude.

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Cocking arm has been gnawed by rats.

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After much time smoothing and polishing. Not perfect but much smoother.

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I had to use slave pins extensively to hold pieces in alignment so I could tap the pins home.

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This was very important with the breech assembly, as it has to be hammered back into the slot with a dead blow soft face hammer.

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A small slave pin holds the trigger spring in place. Unfortunately, shortly after this I ended up losing my grip and the trigger spring escaped somewhere in the shop, without making a telltale noise upon landing.

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So I wound a new trigger spring. Dead simple.

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Although I had to make two, the first (R) being somewhat too small.

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Back in place.

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I forgot about the plate washer that goes inside the grips

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It goes here.

So the pistol is back together, lubed and adjusted. It feels better and seems to have a nicer action. I will say that the above took many hours of work, so again, I would never take one apart if I didn’t absolutely have to.

Monday, August 23, 2010

Magazine for a Crosman 118--Part 2 Final

Back to the 118 magazine.

Searched three hardware stores for a suitable spring. No dice. Gotta make the spring. Bought some various gauges of music wire. Lacking a power feed on the lathe, I opted to wind the wire along a piece of all-thread to make the coils. A foot of #10-24 is about the correct diameter. Ideally, the coils would be further apart, but I'll make do and stretch the spring out. As I needed to anchor the wire at one end of the rod, I cut a slot and chased the threads.

Wire lays in the slot.

Nut threads down and locks the wire in place.

Wind the wire into the valleys of the thread. Need to keep constant tension on the wire--or it just unwinds.

This is over two-and-a-half feet of music wire.

I found out the hard way that the wire will not set to the size of the thread by itself. Gently clamped the wire to the rod with a vise-grip so it couldn't unwind.

Heated the wire with a torch for a moment then quenched.

Removed the nut and unscrewed the spring.

I pulled and stretched it out a bit to get the necessary length then finished the ends. The small piece of material on the right is delrin (or acetal--if you prefer). I turned it to 0.230" to fit inside the magazine.

Then, turned about half the piece of delrin down to 0.160" to fit inside the spring. Left a shoulder for the spring to bear against. This will be the magazine follower. Made some comparisons to the original 118 mag and measured the amount of follower protrusion.

Marked the spot on the new follower for the stop pin that will allow the same extension. Drilled about 3/4 of the way through with a #43. That drill size was chosen to allow a pin diameter that would slide freely through the milled slot in the magazine body.

Chucked a piece of 0.125" brass rod and turned down to 0.090" diameter.

I'll cut off the end to make a tiny rod for the follower stop pin.

Cut a groove near the end of the magazine. This engages a detent inside the 118's receiver, holding the magazine in place.

Knurled a piece of 0.500" drill rod to start the end cap for the mag.



Squared up the ends and machined down one end. Cut a defining edge up to the knurl.

Spotted

Drilled just shy of an inch deep. Didn't break through. The bottom of the hole will serve as the seat for the follower spring.

Eyeballed a good spot for a couple tiny retaining screw holes in the end cap.

Countersunk

Wire brushed the old finish off the body, then transferred the holes from the cap and drilled with a #50.

Tapped #2-56.

Test fit. The end cap secures with opposing #2-56 stainless steel screws.

I'd been pondering (agonizing?) how to lock the follower back to load the pellets. The original 118 mag uses a spring clip to hold the follower. The spring releases the follower automatically by simply inserting the mag into the gun. Mine won't be quite as complicated. I went back to the milling set up and cut a forward slanting angle at the rear of the follower pin slot. The follower pin can now be pulled back, then turned slightly to lock in the rearmost position. After inserting the mag into the gun, it should take just a thumbnail flick to unlock the follower.

Had to play with the height of the brass follower stop. If too high, it won't slide into the gun. Needs to be flush with the diameter of the mag body.

Test assembly.

A few different angles.





Disassembled for finishing.

Blued the cap and body with Birchwood Casey Perma Blue Paste.

Follower locked back.

A better pic of the loaded magazine. Ten .22 cal Crosman wadcutters fit perfectly.

The 118's receiver has a slot to show remaining pellets in the mag. Clever. I'm absolutely dumbfounded that the "prototype" mag functions perfectly. Ten shots as fast as you can work the bolt and squeeze off the shots. As I didn't want to disassemble the original mag for measurements, it was a nice surprise that this worked without endless tweaking and re-work.

Saturday, August 21, 2010

Rebuild of Joe's Crosman 454

Sidetracked from the 118 magazine when buddy Joe asked me to fix a leaky Crosman 454 semi-automatic BB pistol. This is a second variant due to the loop on the CO2 piercing screw at the bottom of the grip--which means it was made right around 1980. The gun uses a 12 gram CO2 cartridge housed in the grip and it holds 16 BBs. The BBs are held linearly above the barrel. A spring loaded plunger pushes the BBs backward to the breech where one is loaded with each trigger pull. The trigger is essentially double-action only with a pull that ranges from about 5-1/2 to 6 pounds of weight.


Joe told me the CO2 was leaking from the end seal.

The right side grip is clipped to the 12g CO2 cartridge and pulls right off. The left grip is held by two screws.

Joe was right. The end seal is almost non-existent.

Removed the rear sight.

Four screws hold the frame together.

Screws removed, the right-side half lifts off.

If you want to remove the barrel, there's a small screw on the underside just behind the muzzle. It retains the front sight--which in turn holds and centers the muzzle.

Of course, the safety ball bearing fired across the room when I lifted that right half. Some things never change. I scrounged a tiny replacement 3/32" ball bearing. (Nick probably still sells bags of tiny bearings for just such occasions.)

Detached the hammer and trigger springs.

Small set screw retains the barrel in the valve. It's a 3/32". Just unscrewed it a turn.

Removed the valve anchor bolt in the left side of the frame.

Pulled the trigger pivot pin, wiggled the valve around then lifted off the hammer. The entire trigger, linkage and hammer assembly comes out as one piece. It's straightforward.

Slid out the smooth bore barrel. If you look at the breech end of the barrel carefully, there's a circlip in a groove that acts as a locater stop against the valve.

The BB follower is plastic. Look at that spring! That's exactly what I need for my Crosman 118 magazine. Think Joe would notice if the gun was gravity fed?

Some valve pics. Rear. The silver protrusion is the valve stem that gets struck by the hammer.

Top. The screw holds a spring that pivots the BB shuttle (for lack of a better term).

Screw and spring removed. The shuttle slides right out. It picks up a BB from above and as the trigger is pulled, a transfer bar pivots the shuttle into alignment with the breech. It's a really simple, elegant design. Note: There are no seals on the side of the shuttle-- just an interference fit in the valve body.

Removed the cap from the front of the valve.

Valve spring and stem pulled out.

Ah, here's that bad cartridge seal. Unscrewed the threaded retaining ring.

Used a dental pick to work the crumbling seal out.

Underneath is a standard 38T/C piercing pin and screen filter.

Here's what the crumbled pile used to look like. Crosman's part # for the seal is 38-128. It's still available and used today in the Crosman 357 pistol.

Reassembled: Screen, piercing pin, seal, retaining ring.

Replaced the cap o-ring with one that looked similar in nitrile. Didn't replace the stem seal. It actually looked pretty good and it operates with 900 psi on it--that really helps keep it closed.

Greased the shuttle's sides to help pivot smoothly and seal.

A couple views.

Oh, I lubed the valve stem seal with a little Crosman Pellgun Oil. The rest of the reassembly was pretty uneventful. I did refinish four or five of the visible screw heads, removing old screwdriver marks and rebluing. The gun gassed right up and fired 60+ shots without any hiccups. I'll give it back to Joe and he can finish giving it a shake down.

If I ever find one of these (and for the right price) it would be relatively easy to turn down 8" of 1760 barrel and shoot this with 0.177 cal lead balls. I'd imagine that the accuracy might even be pretty decent but probably not the velocity.